My Golf is a 10 Millionth Edition (or "Champ" in France), and this limited edition had several very specific options at the time, one of them being the fabric used for the upholstery, a stripped blue that's on no other model (pictured below, from the period leaflet).
Well, actually, this was what I thought, for almost 20 years, until 2 years ago...
I then found out that in 1989, a limited edition of Jetta (the "GLI Helios" edition), of which only 1500 units were made, exclusively for the american market, had also received the very same fabric on their seats.
With a major difference though : it featured very desirable Recaro front seats!
Needless to say, I started hunting for a pair of those, but they're rare as hens teeth, and whenever an ad is published, it' always in the US, with prohibitive shipping costs.
Being my usual stubborn self, I kept looking, for almost 2 years...
Until march 2016, when an auction pops up on eBay UK, a stone's throw away from one of my in-laws! God Save the Queen!
I won't bother you with the details of the organisation set up to retrieve and ship the seats to southern France, but here they are, even nicer than I expected them to be! (yeah, OK, spending that much time and energy for a pair of bloody seats, I know I have a problem, leave me alone!)
Here's the difference between the original "Sport" seats and the Recaro version :
But how the Hell these parts, exclusively made for the US market, made their way to Europe?
Actually, around a decade ago, a US soldier dispatched to an american air base in the UK, decided to import his Jetta Helios... He ended up selling the car there, but unfortunately it got wrecked and sold for parts. The seats got bought and stored for the next 9 years, until their owner decided to part with them. They got attacked by rodents in the meantime, but were neatly fixed by an upholstery shop, with a leatherette matching perfectly the original one.
You know what happened next...
I still needed the railings to install them... I found'em in Poland (damn, eBay is a hard drug), a complete G60 set with electric adjusting (too much? ). Let's do it!
Th passenger seat had that part ripped... That's pretty common on Recaro seats, resulting in the bottom of the seat caving in. Fortunately, you can find a replacement on eBay UK, under the name of "webbing" or "diaphragm"...!
Not that easy to replace though, as it's very tight! My solution finally was to grab each hook with vise-grips, then use a clamp to pull the grips towards the edge of the frame.
And.... TADAAAAAAAA!
I still have to install a bit of wiring and a 20 amps fuse to use the electric adjustment thingy, but I can already enjoy the bloody things!
Dear Martin, thank you so much for your help securing the Glorious Seats!
Bonus : Gearbox linkage upgrade
Keeping on track with the improvement of both user experience and reliability, I decided to make a big update on the gear selector linkage.
The original bushings and links, made of plastic, end up wearing and breaking up (I think I changed mine at least 3 or 4 times). You then get a good 10cm end play on the gear stick, no matter if you've selected a gear or on neutral! You can still use the car if you're used to it, but forget about "race" driving. In the other hand, it's a pretty good anti-theft device!
Long story short, I ordered a "Smartshift 2" kit from USRallyTeam, which replaces all links with Unibal joints, and all bushings with Delrin-made ones (POM). No more end play!
I installed the kit on January 30th 2016, but it left a mark (literally) : as I was cutting off one of the joints with an angle grinder, I made a wrong move and sent the cutting disc into my left thumb. Cut down to the bone (got a nice gouge in it), tendon and nerves ripped... #ERsaturdayNight
Anyway, I spent a night at the hospital, but at least the kit is installed, no more end play in the stick, it feels great!
In the picture below, you can see the ugly original plastic joints and "ball", that usually wear off and break
Second picture is the kit form USRallyTeam :
now we're talking! I don't have a decent picture of the kit installed in my car, as it's not easily accessible to get a pic, but you can have a look on this page if you wanna know how it's installed.
I'll spare you the picture of my post-surgery, Frankenstein-like thumb...
As happy as I am with the result, and if I'd happily recommend that kit to others, it is not perfect either : the hardware is imperial threaded (doesn't make sense on a european car), I did not have the correct bolts (you need 2 left threaded, 2 right threaded,.. I only have 4 left threaded ones in the 2 kits I ordered), and the initial adjustment can be a bit tricky.
In short, not exactly a plug'n'play kit, but a great improvement nonetheless in the end.
Elvira : Rebuilding the 36hp, episode 5 : Fuel Pump
episode 5 : Fuel Pump
Let's continue with the "little things" ; well, "little", but essential! So, I giveth to you, ye Fuel Pump...
I've owned this car for 22 years now, and it has always run this very pump. It was long overdue for some TLC!
After thorough disassembling, I first give it a good cleaning with a brush and some brakes cleaning fluid, to get rid of most of the gunk. By the way, I can see that event though the pump's membrane is completely rigid, it's still in working order and not leaking! Pretty amazing quality part, I doubt the new one will last that long!
Next, just as for the carburetor earlier, I dump all the parts into the ultrasonic cleaning bath, filled up with lemon juice. It looks like new when it comes out after just 20 minutes at 80°C. I rince everything thoroughly with clean water to neutralize the acid action.
Before I put everything back together, I check that both pump halves are actually plane : 320 grit sand paper on my surface plate, a squirt of WD40, and I do 8 figures with each half. Right from the beginning, the sanding marks show it was far from being plane...
Ten minutes later, it looks much better! At least it should limit the risk of leaks right there...
I reassemble everything with a BBT rebuild kit. The membrane (main part) looks good, but on the other hand, I will not use the two small levers provided in the kit (edit 20211017 : spoiler aler : I should have!), they look cheap and flimsy, I'll stick to the original ones that still looks pretty good. The main spring is much longer and strong than my original one ; I don't know if it respect the factory measurements, but if so, my spring was in dire need of retirement!
In order to propermy install the membrane, you need to pre-load the pump ; this is supposed to be done using the VW328b tool (see it here on TheSamba), which I obviously do not own, so I make myself make-do one.
The 1958 workshop manual states that the pump's lever should be depressed by 35mm from the pump mounting plane ; so, a piece of laminated steel, three holes -one of which is tapped-, and there you go.
I finally just have to mount the membrane with a thin coat of grease, so that it slides smoothly in place, avoiding any "wrinkle" that may cause a leak...
And BAM, an as-new fuel pump ! The inside is packed with grease, and it goes back on the engine.
NEXT!
Edit 2021/10/17
Well, finally, I should have used the lever parts from the kit... As the engine didn't start any more, I found out no fuel was coming to the carb, and I found the lever/arm thingy broken. The stronger spring may be responsible for the lever's untimely death.
I put back everything together with the BBT lever, and it works perfectly (even though I still think these stamped parts don't really fill me with confidence). I also re-use my original axle, as the kit's one does look nice with its 2 circlips, but is too short for my pump's body.
Anyway, back on the road!
Edit 2021/10/22
Do you remember when I was saying "The main spring is much longer and strong than my original one"?
Well, I should have stuck with my initial gut felling and kept the original spring. The kit's one clearly puts way too much force on the lever... Which broke on me for the second time.
Except this time, I was on the road, for the first outing of Elvira in 14 years... And I rode back home on a tow truck.
Long story short, bought a new kit, installed new lever and membrane (which did not like the too strong spring either), and this time around I put back the original spring.
Re-fixed, and back on the road.... Again. Hopefully I won't have to reopen this fuel pump anytime soon!
Elvira : Rebuilding the 36hp, part 4 : Solex 28 PCI
episode 4 : Solex 28 PCI Carburetor
Just to change things a little bit, I decided to take care of my carburetor next,
Histoire de passer un peu à autre chose, je m'occupe de mon carburateur, le petit Solex 28 PCI.
After 57 years, it was long overdue for a rebuild...
Actually, I just found out about a cleaning method on a vintage motorbikes forum : they clean their carbies by putting their parts in boiling lemon juice, directly in a sauce pan! And I have to say, I was pretty amazed by the results!
So I tried the same approach, but using my ultrasound tank, filled up with 6 bottles of lemon juice, heated all the way up to 80°C!
So after I disassembled the Solex, I let it soak in for 3 ultrasonic rounds of 20 minutes, after which I rince everything in clean water (ideally it'd have to be warm to avoid thermal shock) in order to remove any remaining acidity left by the lemon juice... Then a quick blow dry. I immediatly lube the rotating parts to avoid any oxidization...
And the result is pretty neat!
I think the ultrasound are pretty useless here, being dampened by the particles in suspension in the lemon juice ; but they still help agitating the whole thing, and it probably helps.
I reassemble the carb with a renovation kit - all the gaskets were dry, the accelerator pump diaphragm completely rigid... It was time to do something about it.
But obvisously, everything was going fine. Too fine. So as I was reinstallint the jet on the emulsion tube, lightly tightening it as I know it a fragile part... Crack. F*ck me.
Fortunately, this emulsion tube can be bought NOS online on eBay in Italy... So 10 days later, here we go again, I replace the cracked tube... (note : there's an alternative to the NOS tube : one can buy a brass made replica at Bob Services : thanks SebCore for the info!)
To extract the tube, I first tap it with an M3 tap, pull.... But only the brass part comes. Second try, I tap the remaining tube with an M5 tap, pull it... And this time it's out. Yes!
The new tube is inserted after heating the carb body with a heat gun (on "low", be gentle!). The tube itself is cooled down with a couple of squirts of brake cleaner fluid + compressed air blow. It's not settling in that easy, so it took some convincing with a small hammer and a drift punch, the carb being held in the vice. Again, gently!
Now I only had to put everything back together with new gaskets, replacing as well the small metal pins on the linkage, with were prone to breaking due to their age.
And there you go, a new-ish carb!
It directly goes into a plastic bag, waiting for the holy day it will make my engine come back to life...
If you're a regular on this blog, you've already heard about "Krapo Bleu" (that would translate as "Blue Toad"), my daily driver for almost 19 years now (ouch, I'm not getting any younger, am I?) : a 1988 Golf Mk2, edition 10 Millionen (or "Champ" for the French market).
As I said in my November 2013 article, its angine was starting to seriously wear out (270.000km... and I'll have to admit, I did not always take good care of it!), eating more and more oil (like a liter a month!), used to leak water, overheat... It was high time to do something about it, and finally take care of my "old friend" that helped my so many times, before I actually end up stuck on the side of the road with a broken engine.
After spending a year looking for the right engine, I finally found in may 2014 a block on LeBonCoin (the equivalent of Craig's List in France), for 200€. It wasn't that easy, as several times people tried to sell me broken engines, with broken timing belt (the valves-in-pistons kind) or blown head gaskets...
This engine is strictly identical to the original one (OK, I know, therefore the term"engine swap" may not be appropriate : sue me!) : 1.8L, 90hp, Pierburg 2E2 carburetor, but scoring "only" 130.000km (barely broken in, right? ). Enough to give my old car a breathe of fresh air.
This engine will wait a little over a year before I finally get some time in my hands to get it in the car.
I've used that year to completely clean the engine, changed lip seals and head cover seal, etc...
It's already July 2015 when I head up to Laurent's (Dangerous) to use his hoist, car lift and roomy workshop (which is a much easier way than using a jack in an underground one car garage!)
So there I go, starting with removing the whole front mask of the car, all the accessories, strapping the gearbox... And the engine comes out easily(-ish)!
At this point in time, my Golf has its engine out, my Beetle's 36hp is still not finished, and the Karmann's engine is not even closed yet... Not very reassuring!
With the engin out, I had room to clean the whole engine compartment from the 27 years of stratified gunk.
Up to this point, everything's going as planned ; with a bit of organisation, it's even simpler than it looks.
Now is time to get the new engine in (after I transferred on it the carb, clutch, flywheel, exhaust manifold, and a couple of things more) : it goes pretty swiftly, except for the exhaust clamps that are a PITA to install when you don't have the specific tool. Nothing a ratchet strap can't fix, though (#ratchetstrappower).
And... That's when things went sour... Argh, why is nothing ever simple!
1st start : the engine starts right on, that's the good news! In the other hand, an heavy water leakage appears on the side of the engine, Bellagio fountains like. Probably because the engine got a shock while being stock or transported (that's highly probable, I had nothing to strap the black in the rental truck, it was a bump ride!)...
I've been told that "when you've got a mechanical problem, the best solution is to do mechanics" (is it Confucius or Plato, I can't remember?) : we get the head out, and put it on the mill, fearing it may have warped. The joint plane is cleaned with only 12/100th of mm, so no, the head was fine, and it can go back on the engine with a new head gasket. Let's give it another try!
2nd start : this time, the intake manifold leaks water (water goes through it to heat up the carb)... It's not the Bellagio any more, but still a solid Manneken-Pis.
I take the intake manifold out, order new gaskets, reinstall everything with sealing compound, making sure it's tight...
I'll have to admit, from this point on, I took way less pictures, I was too busy to play the paparazzi!
3rd start : intake manifold still leaking. Less than the first time, but still leaking anyway.
Re-removing it, re-reinstalling it with again new gaskets and compound...
4th start : the manifold is not leaking anymore! Alleluia!!!
But now, I have a water leakage on the side of the block, behind the timing belt cover... Once again, we remove the distribution, to find out it's a bloody core plug! Has anyone seen this before?? It's not an heavy leak, more like a fast drip, but still...
So we find a new core plug, extract the old one, install the new... And here we go again.
5th start : the engine is not leaking anymore!!! Woohooo!!!
.
.
.
But the radiator is. HOLY MOTHER OF FUUUUUUUUU...!!!!
I mean, not much, a slow drip, but it's leaking nonetheless. It didn't like being taken off... Classic.
Long story short, I order a new radiator, purge the coolant for the Nth time, replace the radiator....
6th start : IT IS NOT LEAKING ANYMORE! At all! Woooohooooo!!!
I was about to call that car "Pissing Bitch" instead of "Krapo Bleu"!
In the end, the operation that was supposed to take us 3 days took 3 weeks (counting the ordering parts back and forth). Oh joy!
A huuuuuuuuge thank you to Laurent/Dangerous for his help, his time... And his workshop that I made a total mess of pouring so much coolant everywhere!
As you can guess, I still had some work to do after this, as the bloody Pierburg 2E2 carb never misses an occasion to act up... It was working perfectly before, but it has a few hiccups : some air intake (even though the flange is brand new), the choke doesn't work any more, etc...
In short, it needed a bit more tinkering around to get it to work neatly : changed the choke dilatation element, put a thin film of sealing compound on the carb flange, changed the head cover gasket that was leaking oil (it was brand new too...), replaced the 3 temperature probes...
But here it is, finally! Working as if it was new! Well, almost!
Elvira : Rebuilding the 36hp, part 3 : Closing the engine
Sorry! This article has not yet been translated in english! Please come back later!
part 3 : Closing up the engine case
QUATRE ANS! Quatre ans que j'attendais que les astres s'alignent pour le fermer ce bloc! E N F I N !!!
Carter moteur
Contrairement à ce que j'annonçais dans mon précédent post (en mars 2012...) sur le sujet, la métrologie du bloc n'était en fait pas si bonne.
En la reprenant à tête reposée avec mon nouveau matériel, je me suis aperçu que les paliers vilo étaient hors-cote ovalisation. Pas de beaucoup, mais j'allais pas remonter le carter comme ça, avec toutes les pièces que j'ai, c'aurait été du gâchis : Bielles NOS, axes de pistons NOS, coussinets de vilo NOS, coussinets de bielles NOS, tubes enveloppes NOS, tôles sous cylindres NOS (!), AAC "Okrasa" Joe Ruiz...
Du coup, j'ai envoyé le bloc chez Feller pour une ligne d'arbre en +0.5mm. Et là, il m'a fallu trouver des coussinets en cote réparation (dommage, j'avais des NOS VW en cote origine dans leur boite!)... Pas évident pour les pieds moulés! Classic-Store en a en stock, mais de piètre qualité (Sintermetal, fabriqué en Argentine), même eux recommandent de ne pas monter ça! ("mais ils ont le mérite d'exister")
Après 18 mois de recherches, je les ai finalement trouvés en Allemagne. NOS VW, 150€ le jeu hors port (ouch!), mais bon, pas vraiment le choix... On est déjà fin 2013, et entre-temps je me suis lancé sur le moteur du KG. Le pied moulé a alors sagement attendu sur son étagère...
Mais c'est fini, il est temps de refermer le bébé!
Janvier 2016, je vais chez Laurent (Dangerous - merci ma caille!) fermer le bloc : il a plus l'habitude que moi, et on sera pas trop de 2 cerveaux pour tout vérifier au montage. Ce qui ne nous empêchera pas d'oublier la tôle sous cylindre au culassage ceci dit...
Ca veut dire aussi un peu moins de photos étape-par-étape, conditions d'éclairage pas idéales dans son atelier.
Mais avant d'oublier, je replace les petites plaques de guidage des poussoirs (qui ont un méplat et ne tournent pas sur pied moulé). Serrage léger avec une goutte de frein filet, et je replie la patte de blocage sur l'écrou. Ca se fait un peu au feeling, le poussoir doit coulisser gras avec un très léger jeu.
Dans la foulée, je reprends la galerie sur le palier N°3 : sur les pieds moulés, le passage d'huile est usiné dans le bloc au lieu du coussinet, et le ré-usinage de la ligne d'arbre l'a sérieusement réduit. Je l'approfondis un peu à la Dremel, sur les deux demi-carters.
Bielles
Les bielles NOS sont d'abord mises au poids, dégrossissage à la meuleuse pneumatique, et finition à la lime électrique : j'ai 0.7g d'écart entre le plus lourde et la plus légère.
Leurs coussinets (NOS eux aussi) sont déglacés avec un bout de tampon Jex usé (à l'huile), installés, et le jeu avec le maneton de vilo vérifiés au Plastiguage.
Le vilebrequin est d'abord rhabillé avec les pignons AAC et allumeur, puis les bielles sont montées dessus, serrées au couple à 5mkg (dixit la RTA et la revue d'atelier, surprenant : 3.5mkg sur T1!), et dé-stressées (petit coup de marteau avec un jet en bronze pour libérer les contraintes liées au serrage).
Au montage, je lubrifie les manetons au Wynn's Supercharge, pour assurer la lubrification lors du montage et jusqu'au premier démarrage. Comme c'est très visqueux et collant, ça ne se fera pas la malle comme de l'huile...
Cylindres / Pistons
Les têtes de pistons sont passées au marbre : polissage pour limiter le transfert de chaleur.
Les cylindres ont été contrôlés en même temps que les pistons : tout est dans les cotes. Clairement le kit n'a que très peu roulé : perso j'ai du faire 2000km max avec ce moteur, je suppose que les chemises/pistons avaient été montés neuf dessus.
Bref, les cylindres sont simplement nettoyés et déglacés (honage), et sont déclarés bon pour le service.
Les pistons sont gentiment préparés : un petit chanfrein sur le bas de la jupe (à la lime electrique : super outil, il m'en faut une!) pour aider la création du film d'huile, angle cassé à la tête (doucement au papier de verre 800), et mise au poids (pas évident, 2 fonderies différentes, j'ai du me résigner à avoir deux plus lourds et deux plus légers, chaque couple mis en opposition 2 à 2).
Je contrôle derrière le jeu à la coupe des segments : la RTA donne entre 0.35 et 0.62, j'ai 0.35 serré sur les 8 segments d'étanchéité, parfait. Je les monte en y allant doucement sur la pince à segments, et en huilant tout bien ; on vérifie bien que l'inscription "top" est vers le haut, on tierce en tenant compte de l'orientation vers le VM (deux ouvertures du segment racleur en haut, décalées de 45°, deux ouvertures segments d'étanchéité en bas à 120°).
Finalement, les pistons sont emmanchés dans leur cylindre respectif avec un compresseur de segments, et beaucoup d'huile.
Culasses
Beaucoup de travail sur les culasses que j'avais trouvées à Valence...
Après un nettoyage en règle à l'essence F, je les ai microbillées pour y voir clair. Pas de mauvaises surprises, un micro-bout d'ailette cassé, rien de méchant ; et surtout, aucune fissure. Banco! ("je l'entends encore... Banco..." : un cookie pour celui qui capte la référence).
A propos : il vaut mieux boucher les guides de soupape pour le micro-billage : un bon plan pour ça, c'est les bouchons d'oreille jetables en mousse!
Elles sont propres, mais bon... Il y a matière à améliorer les choses. C'est pas un foudre de guerre le pied-moul' d'origine, s'il y a un cheval à grappiller par-ci par-là, faut pas s'en priver. Et les culasses sur un moteur VW, c'est le nerf de la guerre...
Alors on se retrousse les manches et on y va!
Pour commencer, les sièges de soupapes sont retouchés trois angles pour améliorer le flux (il y a une vilaine marche d'origine) : faut y aller tout doux, y'a pas beaucoup de viande pour travailler.
Ensuite, les soupapes sont nettoyées et légèrement modifiées : montées sur une perceuse à colonne, et retouchées à la lime électrique. Lissage, la tête un peu diminuée pour retirer le bossage... Le but est toujours d'améliorer le flux ; tout doux encore, y'a pas beaucoup de matière.
Les soupapes sont rodées sur leurs sièges, et les demi-clavettes de queues de soupapes réduites (au niveau du plan de contact, pour bien plaquer sur la soupape ; les clavettes se touchaient et du coup avaient du jeu sur la soupape).
Puis les conduits sont légèrement repris, pour retirer les marches, marques de fonderies, alignement siège/conduit, etc... Dremel et fraiseuse pneumatique, et on lisse tout ça.
Ensuite : d'origine, le rapport volumétrique était de 6.6 (d'après la RTA), ce qui était ok avec les carburants des années 60, mais franchement dépassé avec notre Super 98 : un 8.5 serait mieux, pas de risque de cliquetis, plus de watts et meilleur rendement.
Je mesure donc mon deck height (0.88mm) et le volume de chambre d'origine (48.75cm3) : je tombe sur un RV à 6.64, ce qui correspond bien à ce qu'annonce la RTA.
Pour augmenter ce RV, pas 36 solutions, faut diminuer le volume de la chambre de combustion, et pour ça descendre le fût de cylindre dans la culasse, en vérifiant régulièrement le volume obtenu, et recalculant le RV (à ce propos, il y a une super calculette sur F4E pour ça...).
Entre le centrage au comparateur, le réglage de la tête (automatique, bel outil), les mesures régulières, c'est un jour et demi de travail qui y sont passés.
Au final, en descendant de 3.2mm, on est arrivés à 35.6cm3 de volume de chambre, et donc un RV de 8.51. Woohoo!
Même punition pour l'autre culasse, descendue de 3.15mm pour avoir les mêmes chambres.
Evidemment, avant de se lancer dans cette modif, il faut vérifier la levée des soupapes pour ne pas qu'elles touchent les pistons à pleine levée... Dans mon cas pas de soucis, il doit bien me rester 5mm, je suis large.
Sauf que maintenant, les fûts de cylindres ne touchent plus au fond de la chambre, mais en haut sur la première ailette de la culasse ; on sort donc la "bête à corne" et on rabote de 1.2mm, jusqu'à ce que les cylindres plaquent bien au fond des chambres (on vérifie avec un jeu de cale, 0.2mm de jeu entre cylindre et culasse, tout va bien!).
Par contre, sur la culasse droite (cylindres 1 & 2), j'ai l'ailette qui est devenue vraiment fine, façon lame de couteau... Pas top, mais bon. Je vivrai avec.
Finalement les chambres sont légèrement retouchées à la Dremel pour supprimer les angles vifs que l'usinage a créés (sources de points de chauffe et de cliquetis), et ça y est, elles sont prêtes à monter!
Ouf... Tout ça pour ça!
Sur ces photos, on voit un effet de "vaguelettes" sur la culasse après usinage : l'ailette commençait à devenir un peu fine et se mettait à vibrer sous l'outil se la fraiseuse.
C'est bien beau tout ça, mais du coup le moteur est plus court de 3.2mm de chaque coté! Il faudra donc retailler les tiges de poussoirs pour prendre en compte cette réduction, sinon la géométrie de la culbuterie sera dans le sac... Mais ça, ça peut attendre pour le moment, je reviendrai dessus plus tard.
Pompe à huile
Le couvercle de pompe à huile était bien marqué... Je l'ai plané sur marbre au papier verre à l'huile pour lui virer ces marques vilaines d'usure.
Le corps de la pompe à huile est microbillé, son tenon meulé pour éviter toute interaction avec l'AAC, et ses conduits alignés avec ceux du bloc. La face est légèrement planée aussi, juste pour virer les traces d'oxidation, elle était propre.
Bonne pour le service!
Fermeture du bloc
Pour bosser propre, j'avais déjà microbillé toute la visserie (ouais, je vais me faire un T-Shirt "I ? microbilleuz"), et j'ai passée tout ce p'tit monde au taraud/filière. Les goujons de culasses ont été décapés (au tour, ça va vite), passés à la filière, et peints pour éviter la rouille (dans la famille Overkill je voudrais le fils).
Je n'ai pas fait beaucoup de photos de l'assemblage, il commençait à se faire tard et il fallait boucler...
On prépare donc la fermeture :
Pour l'étanchéité, le plan de joint d'un demi-carter est enduit de pâte anaérobie Loctite 518. Super produit : on peut prendre son temps pour travailler (elle ne sèche pas à l'air), elle est miscible dans l'huile (pas de risques de bouchage de galeries comme avec les pâtes silicone)... et j'adore son odeur!
Les coussinets vilo, et les paliers arbre à cames (pas de coussinets AAC sur pied-moulé) sont copieusement lubrifiés à la Wynn's Supercharge.
Les cames de l'arbre à cames reçoivent une couche de ZDDP ; un peu overkill encore au vu des ressorts, mais bon, tant que j'y suis...
Le bas des cylindres reçoit un petit congé de CAF ; idem pour les joints des tubes enveloppe.
Les écrous et rondelles de culasse qui se trouvent sous le cache-culbuteurs reçoivent une couche de 518 aussi, pour éviter les fuites d'huile par les filetages.
Les tubes enveloppe NOS (merci VW Classic via Slide Perf/Classic Store : 8,30€ pièce, ça pique, mais belle came) sont dégraissés et prennent une fine couche de peinture haute température couleur alu, histoire qu'ils ne rouillent pas direct.
Les tôles sous cylindres sont NOS aussi...
On vérifie une dernière fois, on inspire un grand coup, et y'a plus qu'à refermer :
Et.... Taadaaaaaa!!
Bon, on n'est pas encore sur la route hein, mais c'est une bonne étape de franchie!
La suite bientôt!